Wild Food Handbook
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Last update: 15 June 2006
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Tips
Close the stopcock slowly at the generator to avoid a sudden increase in pressure,
which can damage the pressure gauge, and possibly the pipes.
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Micro Hydro Generator - the Water Baby
The Water Baby micro hydro turbine is part of a hybrid 12Volt power system,
providing electricity during the dark wet winter months, when the solar PV
panels only produce negligible amounts of power on this shaded site. The water
for this hydro system comes from four main spring areas. These springs produce
a trickle of water each, but combined give enough output to run this small
generator during wet spells. The geology is slate shale and clay on a steep slope.
The water table is quick to react to the weather. After a prolonged dry spell, one
inch of rain will make a noticeable difference within a couple of days.
The generator is an impulse type turbine, similar to a pelton, but lacks the
central ridge of the buckets, and is designed for low flow situations.
I started installing the hydro system in November 2004. There were a number of
teething problems with the intake, where the filters clogged up within hours.
After trying out various designs, I am now able to leave it unattended for days
on end, and with the installation of the next filter type I anticipate that very
little attention will be necessary. One other major problem was that the amount of water
from spring #1 and #2 was not sufficient to run the generator in all but the
wettest weather. This meant having to bring in more water from the spring area
supplying the domestic water, a little over 150 meters along the contour. I
had to get more pipe, and with the slight gradient, air locks are a major problem.
The way I got rid of the air locks was to walk along the pipe lifting it as I went
along, keeping the 'bubble' at the highest point, which was driven out when I
reached the end of the open pipe. This process may have to be repeated
when the water level goes down and the pipe gets air into it again, however, I
lowered the collection tank a little, and this additional slope may well be enough
to drive out the air with the extra water pressure. This pipe is only 25mm
diameter, and small diameter pipes are less susceptible to air traps when at
a good slope. The main pipe is a 32mm diameter pipe and runs down a steep hill.
Any air entering the pipe when the water level goes down, is quickly driven out by
water following.
When I first installed the generator, I was hoping to run it off the the spring
supplying the domestic water. As the pipe was already in place, this would have
been a minimal installation. However, the pipe is about 300 meter long and only
15mm diameter, which created such great frictional losses, that the pressure was not enough
to give any output. Never underestimate frictional losses. Good tap pressure is
not necessarily enough to run this generator. As I had to run a new, larger pipe anyway, I
started to look for springs nearer the site, and found a couple of good ones about
200 meter from the site. The advantage is that the two systems don't interfere with
one another, but can supplement each other when necessary. During the summer when
the hydro generator will be turned off (the PV is plenty for the summer), and
water levels are down, the extra source with its independent pipe can irrigate
the garden and keep a pond topped up, as well as feed a moat around raised beds
to deter slugs. I would have been loathe to use my precious domestic water for this
purpose, as the 500 gallons are a reserve which may have to last through a drought,
when the springs go down to a drip. Good permaculture in action, an important
element backed up.
Over the last couple of months since getting the first Watt from the system, I have
been running the laptop computer for up to 18 hours a day creating this website,
which is pretty good, considering a computer uses a fair bit of power. My batteries
are very low now, as the weather has been quite dry lately, and the hydro can only
run a few hours a day, but as I write this, the rain is lashing down, and with more
than an inch, I reckon, there will be plenty of power again in a day or two, with
the batteries back to 100% state of charge.
My power situation was dire before I installed the hydro generator, with the sun
dipping below the tree line again for the winter, so I wanted to get the generator
running as soon as possible. Some of the setup is therefor still to be completed,
mostly fixing things into place, tidying up cables, pipes, making a stand for the
generator and proper housing for it, to include a dry space for the multimeter and
spare nozzles and tools. Also the spring intake area needs to be covered, and filter
screens installed. Those jobs will allow the system to run unattended for much
longer.
I am quite pleased with the hydro generator, though I had some frustrating moments
with its installation. It certainly means more light during the winter, no worries
over running the computer, which allows me to do the writing work when the weather
is bad, and the days are short, leaving the fine summer days to do outdoor jobs.
The measurments taken are approximate, especially the head of water. Also the
turbine needs some more fine tuning, as output can be adjusted, and is probably
not at its optimum at present. Tests with other machines have shown higher output
with similar conditions.
Data
Head from generator to intake - approx. 100 feet
Distance from Intake to generator - 650 feet
Penstock diameter - 32mm MDPE pipe, reduced to 15mm at generator
Distance from generator to battery bank - 80 feet
Cable from generator to battery bank - 10mm2 each
Static pressure - 58 PSI
Pressure gauge - 100 PSI
System voltage - 12V
Charge controller - Trace C35
Typical current produced with available water - 1.9 Amp
Update
Since I baught my generator, the company has made some improvements to the stator with more efficient windings.
The table shows output with the old windings, and also unsatisfactory plumbing. I have just upgraded the
generator with new stators, and taken a few measurments. The results are a great improvement. With recent headline
generating record rain, I am in a position again to run the generator at full output and I can test it with different nozzle
sizes, and over a longer period of time. Paul Cunningham of Energy Systems and Design has found a curious phenomenon
when testing his generator; the output rises after the machine has been running for a day or so. This is what I have found
also. Due to heavy leaf fall at present, I have not been able to take a second measurment on the biggest nozzle, as the
partially blocked flow decreased the available water, and I had to change to a smaller nozzle on the first day. The generator
has now been running two days with the smaller nozzle. The table does not show Voltage, an oversight, and unfortunately
does not allow the calculation of Watts, but the relative gain can still be seen.
I have been advised, that the rather long run of 15mm pipe near the nozzle would reduce the flow somewhat. Next upgrade
is larger fittings. I will test the generator first with the new stators/present plumbing and wiring, then new plumbing, then
bring the generator closer to the house which will eliminating about 80 feet of pipe which runs on the flat, leaving the
cable at full length, then shorten cable to see if and how much improvement any of those changes make. So here the first
figures. The increased PSI may be due to continuous running purging the air in the pipe.
Nozzle no. 8
3.3 Amps
Nozzle no. 7
day one - 3 Amps
day two - 3.2 Amps at 14.2 Volt and 46 PSI
Measurements taken with original generator and system
|
| Nozzle # |
Nozzle size |
US Gal/min |
PSI |
Amps |
| 4 |
1/8" |
3 |
55 |
-- |
| 5 |
5/32" |
4.5 |
52 |
0.9 |
| 6 |
3/16" |
6 |
48 |
1.9 |
| 7 |
7/32" |
9 |
42 |
2.2 |
| 8 |
1/4" |
10.5 |
36 |
2.6 |
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Gallery
Click on images to enlarge and drag corners to maximise

Hydro generator with temporary housing, a plastic container/bowl, and a 4" pipe sleeve and
bubble wrap to protect the metal pipe section from frost damage

The Water Baby micro hydro generator shown with the electrical junction box, the
mounting frame on a temporary support, the pipe inlet with stopcock and pressure gauge.
The Water Baby is available with 1-4 nozzle openings. This is a one-nozzle model, as I have very
little water available.
To reduce cost without sacrificing cable thickness, I opted for earth ducting cable,
and wrapped red tape around the positive cable, as there was no other colour choice.
Temporarily the generator is supported on a steel box on battens, to be replaced by
a more permanent wooden stool type frame, with the four legs driven into the ground.

The pipe is removed in this shot, showing the nozzle end (usually held in with a grub screw),
as well as a spare nozzle with a larger aperture. The generator is supplied with a number of
nozzles, each with a different size opening, used according to how much water is available.
The smallest nozzle will allow about 3 gpm through at a head of about 120+ feet, however, I have found
that the smallest nozzle used with that head, produces no current at all. If the springs
are gushing after a good downpour I have been able to go to the second biggest nozzle. With
the new buffer tank I may be able to use the largest nozzle, when the available water is just
below the quantity needed for the largest one.
The generator body is made of aluminium, and the nozzle holder/nozzle is brass, therefore
there will be electrolytic corrosion where the two meet in the presence of water. You can't
do anything about the water, as there will be some splash back from the turbine, but I stopped
the corrosion by liberally coating the brass parts with vasalin. When first installing the
hydro I failed to do that, and after a few days of not changing the nozzle, the brass part
was jammed solid in the hole, and I had to prize it out with a screw driver. With the
vasalin the corrosion has ceased.
The brass nozzle holder supplied with the generator has a standard thread for UK 15mm/1/2"
compression plumbing fittings. I used a tap connector with a fiber washer, and 15mm copper
pipe and ball valve. However, different brands of compression fittings can have different
thread pitch, so it would be advisable to take the fitting to the plumber's merchant to
try out.

The tail race is a tube I fabricated from sheet aluminium to fit the opening of the underside
of the generator. The edges were riveted together and the lower edge snipped and bent in
slightly to minimize splashing. Still to be done is a caulking seal around the top edge which
would prevent any splash-back to seep into the timber frame. The tube is pinned to the inside
edge of cross struts supporting the generator, i.e. is not directly connected to the generator.

The support frame is made of 1" x 4" rough-sawn soft wood, screwed together at the corners.
Two boards are screwed across the top side of the frame, with a cutout for the 5 1/2" diameter
opening on the underside of the generator. The generator is screwed to these boards, through
holes provided in the corners of the housing flange. The long side boards are extended beyond
the corner of the frame so that any loose cover placed over the generator would have support
on the end where the electrical junction box is mounted on a vertical board.

This 1000 litre tank helps to buffer the flow of water to the hydro generator. If the flow
rate of the springs is just below the amount necessary for a given size nozzle, the tank will
allow the larger nozzle to be used for a while, until the tank is empty. As the spring
continues to deliver almost as much as is passing through the nozzle, the water level in the
tank is only going down very slowly. The difference in electrical current between using one
nozzle size and the next is more than is lost by having to close off the generator briefly
to fill up the tank (less than an hour at 4 gpm). This is especially critical when the flow
is just not enough for the smallest usable nozzle. It means being able to run the hydro
maybe 20 hours a day, instead of not at all.
The blue pipe is the overflow from the spring which supplies my household water, plus
another spring in the vicinity. The white pipe delivers water from two further springs.
The tank was free from a local cheese factory. These tanks hold liquid food additives (rennet and
food colouring in this case - there is a second tank further up) and may be available from
other types of food precessing plants. They come on a palette base, and must be used with the
supporting cage, as they are a bit too flimsy on their own and buckle (tried!). Taken apart for
handling, the parts are easy enough to maneuver, even by one person. I managed to get all parts
up a very steep hill on my own without difficulty.

Connecting up a 32mm pipe to the tank without cutting open the top to crawl inside to
screw on the lock ring of a tank connector needed a little trickery and compromise. The
tank outlet has a screw-top lid with a removable center to be able to attach a short
flanged pipe (the flange is held by the edge of the lid). The tank connector would have
been too bulky in the lid, and would prevent the lid from being screwed onto the tank outlet.
I bought a waste pipe 40mm/32mm reducer compression fitting, sawed off the 40mm end just
above the point where it reduces, leaving a flange which fitted into the lid ring (with a
sealing washer). Into the 32mm end I fitted a flexible connector, as the outlet was facing
a big tree. The compression waste fitting just about fits the 32mm alcethene pipe. A push-fit
connector is too loose. You would think 32mm is 32mm, but in plumbing that does not seem to
hold true, just as 40mm waste pipes are not compatible between different brands. After cutting
off the 40mm end of the coupler, I discovered the a 40mm Osma brand waste pipe fits snuggly
into the flanged pipe supplied with the tank (after cutting off the curved spout end). If
you have wast pipe off-cuts it would be a cheaper and neater option than the reducer.

This silt trap is also the collection point for two springs (#1 on diagram - the thick
pipe - the 'stream', and #2 through the small pipe). The s/s filter is
a strainer from a catering tea urn. Any silt, floating or suspended debris is retained
in the strainer. Any smaller, heavy particle (fine silt/clay particles) will further
settle out in the outer tank. This works fairly well, but does require occasional
emptying. One of the springs has another filtration system at source.

There are a number of small springs along the contour line (#2 on diagram). I chiseled a little
channel along this line, slightly sloping down, and embedded a pipe into some earth
at the end. This was expedient at the time, as my solar panels were producing very
little electricity, but the open channel means a lot of silt and debris gets washed
into the intake container, especially after a down pour. When the spring dry up,
which they do after several weeks of no rain, I will cement the bottom of the channel,
run a perfforated pipe through it, and cover it over with geo textile, also cement
the pipe into a small dam.

The source of this water is on my neighbor's land, so the intake is at the bottom of
a steep little stream (#1 on diagram). The pipe is cemented into a small dam. When building the dam,
I first built a temporary one with clay in front of the cemented one, so the water
did not wash away the wet cement before it set.

Due to the steep open channel leading to this intake (#1), silt and debris is a problem.
Here the pipe feeds into a container within the outer container. The inner one traps
the heavier grit and silt, then the water overflows into the outer one. The
edge of the inner container has a series of vertical cuts to form a comb type edge
to filter out any floating and suspended particles. This works fairly well, but still
requires periodic removal of silt/debris from trap. The next experiment will be a
DIY version of an aqua sheer or coanda intake filter, which filters the water before
it enters the collection tank. It is a grill made of closely spaced wires set at an
angle. The water runs over the top and drops into the intake area, whilst debris is
washed down the sloping wire to be dumped outside the intake container.

This spring also supplies domestic water, which is first stored in a 500 gallon tank a few feet below.
When the tank is full, the pipe from the spring is removed from the tank and fed to the hydro system via
another intake, spring #2 nearby. Without a washing machine and flush toilet, the 500 gallons last
a fair time, and in the summer the reserve has taken me through all dry spells so far. When the hydro
generator is needed most in the winter, the water is usually plentiful, and when the water in the tank is
nearing the bottom, it only takes a few hours to fill it again, leaving the main spring flow for the hydro
the rest of the time.

This is a filter which did not work. It was placed over the pipe outlet hole and
is made of woven s/s wire. The debris gets sucked into the screen where the
intricate surface traps everything. At times the whole filter was caked up with
the kind of sludge seen at the top of the filter in this photograph. A better solution
would be a piece of capped pipe with numerous small holes drilled into it, and the incoming
water allowed to wash over the filter to rinse the debris off. The smoother surface
would allow this.

This was another reasonably successful filter experiment. A piece of 40mm waste pipe
with numerous small holes drilled into the side is inserted into a waste pipe tank
connector, which is attached to the bucket inside-out. The pipe is not quite as high
as the rim of the bucket. The water enters the bucket around the side, silt is
deposited in the bucket and the water starts pouring through the holes into the central
pipe, and down into the intake container below, preventing floating and suspended debris
from entering. As the silt level rises, and holes get clogged up,
the water can still escape over the top, and what little debris finds its way out will
be caught by the next filter placed at the outlet of the next tank. Although it still requires emptying
it needs relatively little attention.

Hydro diagram

Hydro diagram, new pipe runs

Spring intake diagram
Payback period
The payback period is the length of the life of the system. What I mean by that is that you are
being payed back every day with the benifit of light, music, the use of your computer, and whatever
else you use electricity for. Oh, you meant cost? What is the payback period on
your car, a bottle of wine, your TV, chocolat, a vacation......? If you can raise the money to pay for it
without going short on necessities, you can aford it.
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There are practical ideas throughout the site, but here are a few ideas for self reliance you might also like to explore:

Foraging for Wild Food
Download a free list of 350 plants, with additional information on parts used, and how to consume, as well as safety notes. You never know when it may come in handy.

Homemade Vegetable Oil Lamp
Easy and quick to make, and cheap or even free.

Cold Vacuum Sealing
Find out how to cold vacuum-seal jars to preserve food (not just jam!) and keep things dry. Its done
cheaply and uses recycled jars, very simple home-made valves and a simple, widely available
hand pump.

Hydraulic Ram Pump
Rule of thumb instructions for building a low cost, low flow pump without the need for welding, and using
off-the shelf material.

The DCMC Binding System
(Dirt Cheap Milk Carton Binding System) Learn how to make a versatile binder with waste materials. There are many
more useful aids to getting organized in the office craft section .
judyofthewoods.net
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Related pages
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Infrastructure
water, communication, transport, access
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Power
the 12V system, solar and hydro
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Tinkering
DIY projects
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Hydraulic ram pump
low cost, low flow, home made
External links
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microhydropower.com
makers of the Water Baby (also sell direct)
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altenergystore.com
distributor of hydro generators, incl. the Water Baby, also shows pictures of
inside of generator. Warning, slow loading page
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ampair.com
UK manufacturer of a submersible hydro generator for run of river (low head) or towed by boat
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norrisscreen.com
for inspiration for intake screens, page link shows large scale application
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Pico Hydro web site
an academic web site on pico hydro (systems up to 5 KW)
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wildwaterpower.com
an interesting overshot wheel
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www.kimberconsulting.com
Low-Power Computing for Renewable Energy Environments
Linux and Windows Consulting and Software Program Management
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off-grid.net
off-grid forum/blog
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